Y 3.N 88:56-2/94-51
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Inappropriate greasing of double shielded motor bearings |
1 |
Y 3.N 88:56-2/94-52
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Inadvertent containment spray and reactor vessel draindown at Millstone Unit 1 |
1 |
Y 3.N 88:56-2/94-53
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Hydrogen gas burn inside pressurizer during welding |
1 |
Y 3.N 88:56-2/94-54
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Failures of General Electric magne-blast circuit breakers to latch closed |
1 |
Y 3.N 88:56-2/94-55
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Problems with Copes-Vulcan pressurized power-operated relief valves |
1 |
Y 3.N 88:56-2/94-56
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Inaccuracy of safety valve set pressure determinations using assist devices |
1 |
Y 3.N 88:56-2/94-57
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Debris in containment and the residual heat removal system |
1 |
Y 3.N 88:56-2/94-58
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Reactor coolant pump lube oil fire |
1 |
Y 3.N 88:56-2/94-59
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Accelerated dealloying of cast aluminum-bronze valves caused by microbiologically induced corrosion |
1 |
Y 3.N 88:56-2/94-60
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Potential overpressurization of main steam system |
1 |
Y 3.N 88:56-2/94-61
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Corrosion of William Powell gate valve disc holders |
1 |
Y 3.N 88:56-2/94-62
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Operational experience on steam generator tube leaks and tube ruptures |
1 |
Y 3.N 88:56-2/94-63
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Boric acid corrosion of charging pump casing caused by cladding cracks |
1 |
Y 3.N 88:56-2/94-64
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Reactivity insertion transient and accident limits for high burnup fuel |
1 |
Y 3.N 88:56-2/94-65
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Potential errors in manual brachytherapy dose calculations generated using a computerized treatment planning system |
1 |
Y 3.N 88:56-2/94-66
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Overspeed of turbine-driven pumps caused by governor valve stem binding |
1 |
Y 3.N 88:56-2/94-67
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Problem with Henry Pratt motor-operated butterfly valves |
1 |
Y 3.N 88:56-2/94-68
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Safety-related equipment failures caused by faulted indicated lamps |
1 |
Y 3.N 88:56-2/94-69
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Potential inadequacies in the prediction of torque requirement of and torque output for motor-operated butterfly valves |
1 |
Y 3.N 88:56-2/94-70
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Issues associated with use of strontium-89 and other beta emitting radiopharmaceuticals |
1 |