Call Number (LC) Title Results
Y 3.N 88:56-2/94-51 Inappropriate greasing of double shielded motor bearings 1
Y 3.N 88:56-2/94-52 Inadvertent containment spray and reactor vessel draindown at Millstone Unit 1 1
Y 3.N 88:56-2/94-53 Hydrogen gas burn inside pressurizer during welding 1
Y 3.N 88:56-2/94-54 Failures of General Electric magne-blast circuit breakers to latch closed 1
Y 3.N 88:56-2/94-55 Problems with Copes-Vulcan pressurized power-operated relief valves 1
Y 3.N 88:56-2/94-56 Inaccuracy of safety valve set pressure determinations using assist devices 1
Y 3.N 88:56-2/94-57 Debris in containment and the residual heat removal system 1
Y 3.N 88:56-2/94-58 Reactor coolant pump lube oil fire 1
Y 3.N 88:56-2/94-59 Accelerated dealloying of cast aluminum-bronze valves caused by microbiologically induced corrosion 1
Y 3.N 88:56-2/94-60 Potential overpressurization of main steam system 1
Y 3.N 88:56-2/94-61 Corrosion of William Powell gate valve disc holders 1
Y 3.N 88:56-2/94-62 Operational experience on steam generator tube leaks and tube ruptures 1
Y 3.N 88:56-2/94-63 Boric acid corrosion of charging pump casing caused by cladding cracks 1
Y 3.N 88:56-2/94-64 Reactivity insertion transient and accident limits for high burnup fuel 1
Y 3.N 88:56-2/94-65 Potential errors in manual brachytherapy dose calculations generated using a computerized treatment planning system 1
Y 3.N 88:56-2/94-66 Overspeed of turbine-driven pumps caused by governor valve stem binding 1
Y 3.N 88:56-2/94-67 Problem with Henry Pratt motor-operated butterfly valves 1
Y 3.N 88:56-2/94-68 Safety-related equipment failures caused by faulted indicated lamps 1
Y 3.N 88:56-2/94-69 Potential inadequacies in the prediction of torque requirement of and torque output for motor-operated butterfly valves 1
Y 3.N 88:56-2/94-70 Issues associated with use of strontium-89 and other beta emitting radiopharmaceuticals 1